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| Leg Vise Rebuild |
| From the New Jersey Blacksmiths Association |
An Adventure in Leg Vise Rebuilding
Article written and contributed by Tim Suter
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| I happened upon a very old leg
vise at a garage sale, that attracted my curiosity. Naturally it was
ridiculously high priced, which I questioned and received the standard
qualification that "it is old". ( So am I but I’m not worth
more.) Tactfully I explained that I doubted that it would bring that
price as I had seen others in much better condition at venues where
there were interested buyers who would never pay that much. Looking it
over, it had no spring, the handle was a piece of 3/4 bar, bent over at
each end and the screw moved erratically. Leaving. I decided that I
would like to have it for the challenge, if the price was right. I kept
my eyes on it for the next three weeks and it hadn’t moved. I felt the
time was ripe so, approaching the seller with tempting green in hand, I
boldly asked him if he was ready to part with it for a realistic price.
He asked what that would be, I said $25, he said $30. Quick as a hootie
owl snatching up a June bug I slapped the green in his hand and the
good, stout, young fellow even lifted it into the pick-em-up truck for
the congenial old gentleman.
Getting it home I promptly tore it down for clean up and closer
inspection. This was indeed an old and very interesting vise. It appears
to have been made by hand, hammer and anvil, without the use of a
mechanical hammer. The screw box eyes were formed by the leg stock (1
1/2" X 1 1/2") being forged out to 5/8 X 3 X 16 inches, folded
over at about eight inches, the eye formed around a mandrill and forge
welded back into itself, then forged to octagon to round and with the
usual upset at the bottom. The jaws themselves are a separate forging,
forge welded onto the top of the legs. At the bottom of the movable leg
is an offset for the pivot bolt hole. It appears to have been made with
two pieces of the 1 1/2" square stock 3 1/2 inches long stacked at
the inside bottom of the leg and forge welded together. A possible
explanation for the 1 1/2" square stock is that it was a common bar
stock size
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| produced by wrought iron finery forges before
various standard rolled bar stock shapes became readily available late
in the nineteenth century. It was not uncommon for iron bars such as
this to be transported to market from remote Pennsylvania mountain
forges by being bent to conform and carried over the backs of pack
horses. The pivot bolt is 7/8 but tapered for a solid fit into the hinge
side plate, the nut was blacksmith made.
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| Page 13 |
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| The screw box itself was made up
of nine parts. The barrel was a rolled tube 1 1/2" ID X 2" OD
with a lap seam, the bell at the back was made the same with a 2"
ID. These two pieces were then forge welded together at the end and
forged over into a recess in the end plug. The plug itself appeared to
have been made with a roll up of thin plate and simultaneously welded as
it was forged to shape. The three thrust rings were forged of 5/8"
square bar with a lap joint. This joint was not welded. I think the
purpose was to have a tight fit but one that could be forced onto the
barrel. This was all brazed together as a unit along with the female
screw thread inside, and no turn lugs.
I put the screw box assembly in my gas forge and brought it up to
bright orange to melt the brass, expecting to easily extract the worn
and damaged screw thread. Not so, the thread was distorted and tangled
and refused to come out easily, so I bumped it on the pavement several
times which promptly distorted the tube to a point of no return. Now I
had to take it apart to salvage the thrust rings, end plug and no turn
lugs. This was more difficult than you might think. It seems to me that
things that have been together a long time like it that way.
To make the screw helix, I formed that with 3/16" key stock, the
dimensions came out compatible with the screw thread depth and 1
1/2" ID pipe for the barrel. I wrapped the key stock into the screw
threads, carefully correcting a twist that wanted to develop as I
progressed. This was done cold so the helix could spring open a bit to
have a more comfortable clearance with the screw. Six foot of key stock
yielded about eight inches of helix. Next I made a sleeve of .040"
brass that fit snugly around the screw helix. (When soldering or brazing
remember mothers admonition "cleanliness is next to
Godliness") I thoroughly cleaned the inside of the pipe and the
brass sleeve, fluxed them with a paste flux and put the thread helix
into the sleeve.
I wanted to put the screw into the helix in order to assure a proper
thread alignment. The problem would be, how to keep the brass from
fluxing onto the screw. This was solved by coating the screw liberally
with high temp 1500° spray paint. I cured the paint according to the
instructions and ran the screw into the helix. Then the brass sleeve,
helix and screw were coaxed into the pipe as a unit, it was a very snug
fit. The four foot length of pipe was not cut as I wanted a good handle
on a piece that would, otherwise, be awkward to handle with tongs. The
eight inch depth of my forge was just right for the heat zone I needed,
with the screw excess through the back door. The piece was put in the
forge, the forge lit and brought up to heat along with the piece. As it
came up to heat I could observe,
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| Page 14 |
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| at the end, the flux get fluid
then the brass, next the helix come to color and finally the brass flow
to the helix. This happened at a bright orange approaching yellow. I
rotated the piece slowly arid soaked it at this temperature for several
minutes before turning off the forge. (I wouldn’t hesitate to try this
in a coal forge at another time.) When it returned to a black heat, I
took it from the forge and put it in my vise.
Now for the moment of truth, would the screw be free? I tried to turn
it with a bar, no movement, don’t panic! I bumped the bar with a
hammer, again, again, a barely perceptible movement, again, more
movement, a sigh of relief. Continued teasing and the screw was out.
After fully cooling the screw was teased in and out several times and as
the flux residue was broken up the action became increasingly smoother.
The pipe was cut to length and the end forged over and into the groove
of the end plug, using a torch and localized heat. A short piece of
2" ID tail pipe was forced over the 1 1/2" pipe to form the
bell, forged over and gas welded to the 1 1/2' then planished to a nice
transition into the contour of the end plug. The thrust rings and no
turn lugs were brazed individually to the assembly with the screw back
in place to assure preserving thread alignment.
I used a 3/4 X eighteen inch piece of 5160 for the new screw handle.
A band of 1/4" X 1/2" was arc welded with a generous fillet at
both sides then forged into a suitable ball at each end. The purest
could do this in his forge by making a half round with 1/4" X
1" in a swage for the bands. Some jaw mis-alignment was corrected
with heat and hammer work at the hinge lugs. The jaw spring of course
was no challenge to make.
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I had an educational experience,
I have a good post vise from virtual junk
and best of all I had fun. Tim Suter. |
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